Dependable HVAC & Plumbing Services In Falls Church VA
At Vito Services in Falls ChurchVA, we take pride in being the leading provider of heating, ventilation, air conditioning (HVAC), plumbing, and air quality management. Our comprehensive range of services includes everything from urgent repairs and precise installations to regular upkeep. Our team, driven by a commitment to excellence, focuses on enhancing the comfort and efficiency of your living spaces. We ensure your home remains warm in the winter, cool in the summer, and the air quality remains top-notch all year round. We also offer plumbing solutions that keep things flowing as they should so your family remains comfortable. Our expertise lies in catering to your specific needs with a dedication to superior service and customer contentment. Choose Vito Services to enjoy the assurance that comes with entrusting your home to Falls Church’s most capable hands, and let us improve your living standards because you’re entitled to the best.
We are excited to welcome you to explore our wealth of positive feedback from our satisfied clients. Every 5-star review reflects the outstanding quality and commitment we invest in each task, regardless of its size. Through these personal experiences, you’ll get a glimpse into what sets Vito apart and the reason why the Falls ChurchVA community relies on us for not only solutions but also for comfort and contentment. Experience firsthand the excellence and dedication that distinguish us by reviewing these testimonials. Become a part of the Vito family today and discover the remarkable service we pride ourselves on!
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Job Locations and Reviews
PARRIS is fabulous! Always a pleasure to have him doing the work.
System is a 2014 Water coil/AC system. Checked all components for proper operation found no issues with components. Secured any loose wires and checked for dirt and debris. Found blower is clean along with evaporator coil. Confirmed all water alarms are operational. Checked condenser unit for proper operation. Checked all starting components found starting components working. Check refrigerant level and found system good. Final cycled system at the time system is operational. Fully checked heating and cooling system. View visual findings from this job at https://www.vitoservices.com
Arrived on site to look at a hose bib that was not working, hose bib was spinning and not closing, took apart most of the hose bib and found a repair kit online, repair kit will need to be ordered and customer wants a quote to make repair, will send customer quote before moving on job, cleaned up work area and left Returned on site to install repair kit, repair kit has not fixed main issue, called tech support and got recommend another repair, customer agreed to order other part and try another repair, ordered part, cleaned up work area and left Returned again to install another repair kit but this time replaced multiple sections of the hydrant, replaced the actuator, rod, and vacuum breaker, reassembled the hydrant and turned the water back on, hydrant is able to be shut off now, showed the engineer, cleaned up work area and left
AC MAINTENANCE ON ONE UNIT INSTALLED IN 2022: Both the furnace and condenser are in the main utility closet on the balcony. I checked both filters and found only one had been replaced upon today’s arrival, I replaced other filter with one that the client provided. I checked indoor blower wheel motor housing for any obstructions and found none. I checked blower amps and found within specs. I checked EVAP coil and found clean and okay. I checked condensate drain pan and EZ trap safety switch and flushed it down with a gallon of water and added Condensate tablets to ensure proper drainage. I checked all other limits and saftys and all wiring and connections were found okay. I checked temperatures and I got a split temp of 18 degrees. I proceeded to check the outdoor condenser unit coil was okay. I noticed the disconnect box outside does not contain a surge protector, meaning that as of right now the unit is exposed to any high voltage power surges. I checked liquid line temp and suction
Spring A/C Maintenance: Checked filter 16x20x1, checked indoor blower motor and wheel found no ecm motor surge protector, checked condesate pan line and ez trap with safety switch, added condesate tablets, checked carrier 120 volt uv light found working at this time, was given the wrong uv bulb to replace, will order correct bulb, checked return air 72° checked supply air temperature 54° , checked condenser motor and coil, checked contactor and capacitor, checked all electrical wires and connections, checked outdoor air temperature 66° , checked discharge air temperature 76° , checked freon level liquid line temperature 76° , suction line temperature 41,
Kitchen sink clogged, used auger to clear drain, ran water for 10 minutes no backups occurred, pipe is clear
System is a 2017 80% Furnace/AC system. Checked all components for proper operation found no issues with components. Secured any loose wires and checked for dirt and debris. Found blower is clean along with evaporator coil. System does not have an Air Scrubber or Humidifier. Checked condenser unit for proper operation. Checked all starting components found starting components working. Check refrigerant level and found system good. Final cycled system at the time system is operational.
Arrived on-site for a plumbing maintenance. Started by flushing the heater, and while flushing, I looked around the house. The customer mentioned two issues: the sediment filter on the footer needing replacement, and that the hot water in the shower gets cold after a few minutes. I inspected the shower and found that the pressure balancer was faulty. I shut off the water, removed the shower trim and handle, and took out the cartridge to access the pressure balancer. After confirming the brand, I reassembled everything. However, when I turned the water back on, it started leaking. The customer approved the replacement of the pressure balancer. I went to get the necessary parts, returned, and installed the new pressure balancer according to the manufacturer’s specifications. As of ticket completion, no leaks were found. I cleaned up the work area and disposed of all work-related materials. Thank you for choosing Vito. Work is warrantied for 40 days.
Commercial Plumbing Job: Leaking Underground Pipes, put camera down line hydro-jetted remaining remnants
For this job I did a AC maintenance on a 2010 carrier AC unit which is at its last life but still running capacitor wa reading within range contactor reading 24 v but shows signs of burn out indoor unit blower wheel amps 1.1 found no signs of obstructions. Sent checklist to client
arrived on site for a plumbing inspection customer said he has a few concerns his water heater, water hammering looked at heater and tested water pressure hose pressure is at 75psi which by code is high also heater is 10-15 years old while talking to customer he said he was thinking of a tankless unit since hit water takes a long time to reach there master bathroom told him he won't need that and explained what a recirculation pump is and how it works and also notice customer doesn't have a liner as well found no other issues in the house have customer investment options and customer said for today he will get other quotes and will call use back thank you for choosing Vito.
Upon arrival customer concerns system is not working. Went to tstat and turned heat on. Went to furnace and found no response on system. Tested all zoning motors for proper operation. Found all are working correctly, Tested zoning board as well and found operational. The call for heat is being made and sending the signal to the board but the system is still not coming on indicating the board has failed. System is a 2011 90% Furnace/AC. Life expectancy of a Furnace and AC is 10-15 years. The furnace becomes dangerous the older it gets and the AC refrigerant your currently using is being fazed out. Because the age(14) and condition of the system it is recommended to replace the system. All parts on system have been superseded to a newer models making it harder to find parts. Cost of Repair is $3000 for parts and labor.
arrived on site, contacted the customer. met up with the customer in the hallways and proceeded to where the pump was located. the pump is located on the 1st floor in suite 150. once inside the customer showed me that the pump is located under the sink. the pump was unplugged. unscrewed all 9 bolts on the tank lid to get access to the actual pump. unbolted the 1 1/2 inch fern that's connected to the pips to remove the lead. once the lead was removed I can now get access to the old existing pump. gently took the old pump out and unscrewed the male adapter for the discharge line unboxed the new pump and assemble the old existing discharge line. bolted up the top of the lead and reattached the fernco's and tested for leaks. no leaks occurred. ran sink until the tank filled up which would activate the pump to turn. no leaks , the pump is functional. pack up equipment clean work area and left job site. thanks for choosing Vito 🙂
arrived on site to take a look at a leak coming from the sink in room 150 on the first floor, took a look around and found the leak to be coming from the under sink pump, pump was constantly running with a low hum noise, took apart the pump and tested it, no amount of adjustment or cleaning would cause the pump to start working, emptied the pump and informed customer of findings, customer wants a quote to get the pump replaced, put the pump back together and cleaned up area, collected the $90 dispatch charge
arrived at location to repipe steel pipe feeding the recruiting pump that is on a cooler tower system. old pipe was broken and corroded. we replaced with steel, this occured in the mechanical room. installed flange proved by customer and pipe the rest out to a section fo no corridored steel pipe. mega pressed and pipe the rest into copper, systems.is back on working at 60-80 psi no leaks occured, installed customer provided gauge as well.
- arrived at location for toilet wax on the 6th floor women bathroom, went up and started to take apart the caulking, found out it was silicon on tile wall in which removed with the toilet a piece of tile included. replaced wax and wasn't able to turn on water due to the sloge vale needing to be repair, maintenance will handle it. - arrived at location for 10th floor women bathroom toilet leaking, aging the silicon made it a bit harder to take off the wall but I managed to take it off without any tile coming as well, replaced wax ring and tested it after testing noticed that the nut for the outlet of the sloge valve was damaged and crossed threaded before, try to put it back with grease seeing if it would help it but it was still leaking , let the maintenance know and they will figure it out they said. - arrived at location for 3rd men bathroom urinal leaking, took it off the wall but as the other on there was silicon behind it, managed to take it and noticed that the wall is breakin
arrived onsite, replaced existing Kohler kitchen faucet spray head as a courtesy to customer. ran faucet and checked for proper operation and leaks. next, began work on upstairs bathroom 2 handle widespread lavatory faucet with cross handles (eventually was able to determine faucet was Danze which has been acquired by Gerber - therefore faucet is discontinued and it is difficult to find parts). removed faucet hot supply hose from brass Y fitting to have better access to hot side repair. with hot side valve body completely removed, inserted it through leftmost hole while holding from underneath sink and threaded top lock nut from above to set stem at proper height for escutcheon/metal base and handle to touch. reconnected valve body supply hose to spout Y/tee fitting. secured mounting hardware and locknut screws underneath sink. with valve body at correct height, replaced existing stem with new Gerber stem and placed in corresponding slots. applied grease to all male threads on valve bo
Pipe to Washington Machine Clogged: The customer notified us that her floor drain would back up every time she washed clothes. Upon arrival, that said that the water level has gone down, and it's no longer backed up. Once inside of the basement, I can observe that the floor drain water level is too high. I advised the customer that the drain is still backuped. Upon further investigation, I flushed the toilet and ran the faucet that's located in the basement to see if those drains were connected. In fact, they were. I went to set up the k-50 to dry thlo tackle the blockage from the floor drain. but unfortunately, after several tries and attempts, I was unsuccessful with clearing the blockage front the floor drain. I went outside and I located a clean out. upon opening g the clean out I can see standing water which indicates that there's a main blockage. set up 1500 and went approximately 150ft . after serval attempts I managed to clear the blockage. went back Inside of residence to
Arrived at location, Customer wanted us to search for the Main Shut off Valves to the building from Unit 148, Unit 150, and Unit 156. We were about to find the Main Shut off valve for Unit 148 which is located in the bathroom. The Main Valve for unit 150 was located in the basement. The main shut off for unit 156 is outside.
Burst Pipe At Central Plant: arrived at location for a busted steel pipe, I was previously out here looking at it, steel pipe was badly cracked and corroded. replaced bad section of pipe with copper since the bottom part is copper. since we used glue to connect the PVC we recommend to not turn on water until the next day at this time to let the guy set and avoid a burst in the pipe. also supported pipe as well since the copper is heavier then the PVC pipe to prevent any future damage of weight etc.
arrived onsite, customer noticed another leak on push pop-up tailpiece even after we both viewed it to be leak free after initial install. leak was coming from drain body/assembly connection to chrome tailpiece. loosened PVC nut from trap adapter and raised plastic reducing slip-joint washer. unscrewed tailpiece from pop up drain body. applied megaloc to male threads on chrome tailpiece and hand tightened into pop up drain body. used pliers with rag to tighten chrome tailpiece (to protect chrome finish) another quarter turn. also replaced PVC nut with 1.5" plastic slip-joint nut and 1.5" x 1.25" reducing rubber washer. applied megaloc to trap adapter male threads as well. tightened plastic nut and ran faucet to check for leaks. moved onto leaking 2 handle widespread faucet in master bathroom. initial leak was from underneath hot side handle. turned water off at angle valve. loosened cross handle set screws and set aside handle. removed chrome escutcheon to reveal bonnet nut and brass l
arrived onsite, disconnected kitchen sink pvc p-trap and applied pipe sealant to threads. reconnected trap to disposal drain arm and trap 90. ran kitchen faucet and checked for leaks. filled k/s approximately 3/4 full of water and released stopper. no leaks on trap and drain assembly. next, removed existing powder room toilet flapper. installed Korky ultra flapper and set band & dial to proper setting for Kohler Wellworth 1.6gpf toilet. flushed toilet multiple times to check for proper operation. recommended customer replace existing pop-up assembly in upstairs bathroom with standard tub/shower. removed existing pop up assembly without disturbing existing p-trap. however, the existing female trap adapter was slightly damaged during removal of chrome pop up assembly. cut below damaged trap adapter with sawzall. cemented new female trap adapter on 1.5" PVC tailpiece above trap. after using sawzall to cut pipe, noticed existing 45 degree elbow going into wall was loose. cut out small sect
arrived onsite for annual plumbing inspection. flushed water heater and checked to make sure all fixtures are in proper working order. first, noticed that the kitchen sink trap was not appropriate for a bigger fixture such as a kitchen sink. the existing plastic tubular trap is better suited for bathroom/lavatory sinks. customer went with my suggestion to upgrade to a PVC trap. first, removed existing trap and unhooked garbage disposal and set it close by underneath kitchen sink. used sawzall to cut out existing trap adapter that was serving the tubular trap. took measurements and cemented a piece of 1.5" PVC pipe to the new p-trap. connected to existing drain line with fernco coupling. rehung garbage disposal and secured it tightly to existing bracket. applied pipe dope to threads and tightened all connections. ran kitchen faucet and checked for leaks. filled up kitchen sink about halfway with water and released stopper to ensure newly installed drain is leak free. my next suggestion
Arrived at location for Multiple quotes customer requested. Starting with the Boiler Condensation Water Line. Seems Like it is leaking from 1-1/2 gate valve, below it is a check valve and gauge attached to a Tee. The gate valve going down to the 90 converting to SCH 80 PVC piping would need to be replaced. (1st quote ) Under those the things, Is another pipe line that is going to into a commercial pump. Customer concern is replacing two 90s due to the corrosion of the material which is 2 in steel pipe.(2nd quote) Customer would like a quote for urinal and two hang-wall toilets, gasket repairs for all three. (3rd quote ) 3rd floor- urinal wax ring replacement ( kohalr ) closes to the wall. 6th floor- women bathroom wall hung toilet wax replacement(1) 10th floor- women bathroom wall hung toilet was replacement (1) customer will like 3 separate quote for these items.
Backflow Preventer Testing: Came out and performed the extensive flush which removed a lot of cloudy water and some granular hard material. I had to reinstall the old second check in order to get a passing mark. The assembly passes now.
New Hot Water Heater Installation: arrived on site to replace the water heater for the tenant, cut off water supply and drained the heater, cut out the heater once empty and carried it out to the parking lot, put the new heater in place and installed it, hooked it up water and gas and started filling it, no leaks, turned on the heater and it started heating, cleaned up work area and left